Thank you guys! After nearly 24 hours of all-out panic, I have it all running, drip free and seamlessly! I have yet to hook up the calcium reactor 100% because I have more top-off water from the large surface area (more evaporation). I think that I am going to put the kalk on a timer and run an additional aqualifter just for the ATO so that no matter what time of year/temperature, the same amount of kalk is being dosed to the same consistency.
Getting the two systems connecting was not as smooth as I was hoping for. I had the vortechs running in the display but nothing else. My first big hurdle was getting the two bulkheads for the overflow plumbed into the new filter sock tub under the display. Getting the tub in there and plumbed to the crossover pipe was cake-work after removing the original LPS refugium form the left side. I made a huge mistake in thinking that the original return pump was not glued inside the overflow. I glued the 3/4"-1" adapter to the bottom and then glued the dual-union valve to that and closed it so that I could pull the stand pipe from the top to trim it... It was stuck. I couldn't remove it now from either side. I stuck my smallest PVC cutter down a few inches into the overflow and started cutting it at an angle and the blade broke... The cutter was stuck inside the overflow, wedged on the pipe. I struggled for an hour trying to get it out without break the glass and wound up making a tool to free the broken blade. I made a rectangular piece of aluminum to slide down into the 3/4" pipe and then twist to push the blade back out. I then got smaller cutters to make the cut and re-secured everything. The other drain went smoothly.
The next set of issues came when I turned it all on for the first time. I had a few drips at the manifold caused by me running with all of the valves mostly closed to dial it in. Everything was under too much pressure. I finally decided after attempting to fix many leaks just to have them leak again, that I would open up the valves and hope for the best. "The best" wound up coming in the form of the return pipe for the 12 long being pointed too high and it shooting water over the edge across the room. As soon as I plugged in the pump and heard the gargle of the air escaping, I looked up and saw the return pointed up and ran to it, catching it just as water was flying at me mid-air. I got it pointed down just in time to get everything on the granite top, me and a good portion of the ground wet without losing any significant water. The tragedy of it all was my open bag of candy hearts.... There's always next year. :sad1:
After getting it all going with the valves all open, I didn't watch the 12L close enough and overflowed it slightly. After that, I dialed to a good spot and then turned it back a little for wiggle room. The display is wide open as was the GFO for a good portion of the night. I wound up dialing the GFO slightly back when I woke up and saw the sponge from the bottom almost all the way to the top. I removed the reactor, cleaned the sponge and put zip ties on the inner pipe to hold the sponges down. The reactor can handle a lot of flow, which is good because it supplies the frag tank with water. I still had a couple very slow leaks on the manifold which "repaired" themselves overnight. The fan and power supply that I got for the pan world pump wound up being a huge frustration because it didn't work. I tested the power supply to find it producing the advertised voltage on all settings... I tested the fan and found an open... Just for the hell of it, I switched the leads and got continuity, meaning that they installed the diode inside of it backwards... whatever.. I switched the wires up and ran it in the reverse direction. It was a little louder than I would like so I decided to run it at 9v instead of 12v and it still keeps the pump cool to the touch.
That's all of the update I have for now. I will return with pictures soon.